and into February !
Hi
We (John and Brian), were pleased yesterday to be able to reconnect the final few panels of the nine that we took up to refurbish along the old ‘Tunnel’ section and it’s looking good, a nice flowing curve. We can now top up the ballast and level it all through…… then we can run some trains.
Meanwhile Peter, Kevin and Brian B endeavored to remove the safety valve on Peter’s ‘Prospero’ , (they did in the end !) so as to ensure we have the correct fitting to enable Brian to come and carry out the necessary tests to keep the loco’s certification up to date.
….and we have started to degrease and clean the ‘Shay’ s chassis so we can check all is ok underneath then we can put it all back together and have a run !
Busy January !
Hi there, well the ‘near future’ was nearer than we expected, for the track along the old tunnel section has been lifted and the sleepers were found to be in very good condition. So they were transported to the workshop area where they were checked over and brushed off to get rid of any mud and soil and now they are drying out so they can be creosoted before being relaid. The ballast has all been removed along that section too.
The other good news is that we started the Shay’s new engine on Saturday after checking that everything was ok and ready, and it sounds , quietly, very good, and the loco was moved slowly up and down to ensure the drive belt was fitted OK. Excellent progress so we can now continue with the general overhaul , cleaning and repainting as required….
John, Kevin and Andrew checking the lifted track sections
Inside jobs !
The weather was rubbish again on Wednesday so we spent the day inside making up a drilling template to locate the track fixing screws in the right place on the sleepers when making up track panels. We intend to replace the sleepers on the old Tunnel section in the near future once the creosote has dried off the newly treated sleepers a bit. Interestingly, we have found that there is virtually no penetration of the creosote into the sleepers that were in the creosote bath for a couple of weeks, so we are just going to brush coat the sleepers in future. Could be that the timber is tanalised and that the creosote has some oil in it ?
Peter’s Class 08 is now serviceable again after having its loose axle (s) sorted (with Kevin’s help), having been thoroughly cleaned and oiled, its body replaced on the track in the workshop and tested, all good…
and the Shay’s exhaust now has a length of 28 mm copper pipe soldered on , thanks Keith, ready to fit back into the boiler, hopefully tomorrow?
Mince Pie specials
Richard with ‘Viceroy’ and Andrew
Hi there, we thought it would be nice to run a few ‘Mince Pie Special’ trains last Saturday to celebrate Christmas, so the day, which was dull, misty and mostly dry, saw ‘Isabel’, ‘Prospero’ and ‘Viceroy’ out and about with several of us having a drive in the very atmospheric conditions until we had had enough at which time it was decided to separate the tenders and take the locos up to the top workshop for their warm winter storage just in case it turned cold over the Christmas and New Year period. So a good day was enjoyed by us all, and we were also joined during the day by some of Peter’s family who also enjoyed their visit too, even Stuart was allowed to drive ‘Viceroy’!, There was much ‘mardling’ over some mulled wine, teas and coffees,and the satisfying consumption of mince pies, sausage rolls, and other tasty offerings!
Happy Christmas everyone !
Looking ahead
Peter leaf clearing
One of the jobs we need to do on the railway, is to replace the sleepers and edging boards to the old ‘tunnel’ section as the timbers are not in a a good state, as this part of the track was always damp as the water drained down the gradient here and it was always a shady spot. So some timber has been procured, and on Saturday John and Brian cut it up into sleeper lengths and placed the equivalent of about three track panels in the creosote bath. We had made a mesh ‘basket’ frame to lift the sleepers in and out but this needed a minor ‘mod’ for it to be effective. Peter, meanwhile was busy on leaf clearing duty!
Busy Saturday
The shorter siding with the new route under to the new soakaway seen alongside the wheelbarrow
Hi , despite the rubbish cold, very, and wet weather last Saturday, we managed to get quite a lot done. John, Ben, Peter and Richard did some gardening ‘tidying up’ and with the help of a mechanical digger, (well driven by Ben) extended and backfilled the new soakaway from the storage shed water tank out into the tree belt. (Previously we had shortened and straightened the track coming out of the back of the loco shed, so its just long enough for a loco to stand alongside the water tank.)
Meanwhile, Keith, Kevin and Brian did some more work on the Shay, forming an aperture (posh word for hole !) in the boiler top under the rear dome, that will enable us better access to fit the exhaust, and worked out a method of running the exhaust back into the boiler to the silencer enabling the exhaust to be emitted out of the chimney as before. We also established that the belt drive from the hydrostatic unit under the Loncin can be the same as the original so a new one can be obtained.
Shay Boiler hole
A good meeting !
On Saturday we held our first EVFR AGM which went very well with our accounts presented and agreed, as were the the members’ subscriptions for the coming year. A brief summary of our projects was outlined and then the meeting was closed with refreshments taken followed by some trains out and about. Lucille,Viceroy and Chieftain were given a trundle round the circuit and we were were pleased to see Kevin, who has joined us, having a drive too !
A good day